Subject: NAS2-99090 September monthly report
Date: October 3, 2000
Most of the work effort for September was directed
at testing the rotor to determine what was required to produce a smooth
stable rotor from startup through 425 RPM (max jump take-off RPM).
The rotor is now smooth and stable at any flight RPM
between 75 and 425 RPM.
This was achieved by adding a spar stabilizing bar
at the hub whereby weight could be added 24" on either side of the
spar spanwise centerline. The weights fit inside the rotor spinner.
A form of cyclic dampening was also required. Hydraulic
dampening at the rotor head, not at the control stick end of the push/pull
control cable, worked. However, a very reliable and simple solution was
to increase the stability margin of the blade, i.e. increase the distance
the blade dynamic center of gravity (CG) is in front of the blade aerodynamic
center of lift (AC). This was accomplished by adding a trailing edge extension,
which moved the AC of the blade rearward. Note it may be that; 1) given
enough dampening or 2) a stiff enough cyclic control linkage or 3) the
use of hydraulic boost that neither the stabilizing bars or a blade with
a large stability margin would be needed.
In order to keep the spindle/stick stable during rotor
spin up when 2000 ft-lbs. of torque is accelerating the rotor, an additional
spindle stabilizer bar located 90 degrees to the blade teetering axis
was needed. This is because any time the drive U-joint is not straight,
torque tries to whip the spindle around and feeds back into the cyclic
stick. This is only a problem during spin up, as once the aircraft is
in the air, the rotor is in autorotation.
Both the spar and spindle stabilizer bars acts like
gyroscopes to make the spindle inherently stable without dampeners or
a stiff cyclic control. Fortunately it did not take much of a gyroscope
to provide the stability needed and any gyroscopic precession forces 90
degrees to the stick movement are not large enough to be noticed.
The aircraft is now ready to fly. We have four new
pilots, so we plan to take the testing slow until they gain confidence
and experience.
Note at one time when we could not run the rotor over
150 rpm without experiencing an instability, we assumed the problem was
because 3 items (mast lateral, blade torsional, and cyclic) had a natural
frequency multiple near this rpm. To change the natural frequency of two
of the items we added +/- 45 degree carbon to the outside of the blade,
which more than doubled its torsional stiffness in places, and operated
the rotor with some blade pitch to increase its coning and move its CG
closer to the spindle tilt axis. Neither change, collectively or by its
self, had any measurable effect.
In addition to the time it took to find a solution
to the rotor system stability problem, we had problems with the prerotation
drive that had to be resolved. During max rotor overspeed, the constant
velocity drive runs at a high RPM which forces all the lubricant to the
outside, starving the inner part of the bearings. We had several bearing
failures before we realized what was happening. If a small amount of grease
leaks out of the boot, the bearing fails.
We also had a gearbox failure. We used a ring gear
and pinion out of the salvaged rear end of a small vehicle. The stress
analysis on the gears indicates they should handle the load provided the
gear did not already have a fatigue crack and that the gears are made
from a material with a tough high yield core. Until we replace the gears
with new ones and can perform more tests, we plan to limit the torque
into the gearbox to 75% of what it was tested. This means we will not
be overspinning the rotor but to 375 RPM maximum instead of the design
425. We should still be able to perform zero roll takeoffs and landings,
but they will not be as dramatic.
We also took time to show the propeller to a potential
licensee, (name withheld). They sent four of their senior management personnel
to Wichita Falls in order to review the prop design in more detail and
witness the calibration and static thrust tests on the propeller. The
static thrust from 275 hp was measured at over 1500 lbs. They were suitably
impressed. The CC 4-bladed prop for their turbine engine should not weigh
over 60 lbs resulting in a very impressive total package.
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