PRESS RELEASE, December 23, 1999
Wichita Falls, Texas: Thursday, December 23, 1999
THE CARTERCOPTER SUFFERS DAMAGE
On Thursday, December 16, during flight testing at Olney, Texas, the
CarterCopter suffered substantial damage during an emergency, forced landing.
The aircraft landed at a relatively high forward and vertical speed. The
landing impact caused the nose gear to compress too far, allowing the
nose boom to dig into the soft asphaltat the edge of the runway. The dipping
nose and other factors caused the rotor to hit both vertical tails, the
horizontal stabilator, and the prop. The aircraft spun sideways around
the implanted nose boom but the right wing prevented a roll. The right
wing was broken in the process. The rotor hit the ground after the aircraft
spun around, breaking several feet off each end.
FIRST FLIGHT
The accident occurred during the first flight of the day -- after 2½
weeks of down time. The plan was for the test pilots, Don Farrington and
Jay Shapley, to make a few conservative flights down the runway to get
the feel of the aircraft again before making a traffic pattern and starting
the flight test program. Don, as PIC, was to pre-rotate the rotor to only
450-RPM instead of the usual max of 550 RPM. The rotor collective stop
had been blocked for the first set of tests to have 5 degrees of pitch
with the collective full down. As soon as forward airspeed reached 30-MPH
(approximately 2 lengths of the aircraft) Don was to quickly pull full
collective (10 ½ degrees) and hold it until the rotor dropped to 350 RPM.
At this point he would reduce collective to 5 degrees for the remainder
of the flight. He would then continue with full throttle and climb at
75-MPH. As the end of the 5,000-foot runway approached, Don would reduce
throttle and land.
Don had previously flown the aircraft in steady, smooth, climb outs at
up to 7.5 degrees collective. The strategy for this first flight was to
quickly use the excess energy stored in the rotor and thus get the rotor
RPM slowed down to where it would operate most efficiently (less drag).
What we did not expect was how dramatically this tactic would improve
the aircraft's performance.
CAUSE OF ACCIDENT
Following the pre-flight briefing and before the flight, there were three
separate delays that caused distractions for the task at hand. This was
not a concern at the time since everyone was expecting a short flight
down the runway similar in most respects to those done numerous times
before. Neither the pilots nor ground control noticed how fast the aircraft
accelerated. Don did notice he was having to hold a higher forward stick
force than normal, but was not concerned at the time, and let go of the
collective to support his other hand on the stick.
The collective has a new air boost cylinder, which automatically drops
out at 350-RPM and lowers the collective approximately 2-1/2 degrees.
When the pilot's hand is on the collective, he can feel when the boost
drops out and knows it is time to reduce the collective without having
to look at the instruments.
This time Don did not have his hand on the collective and was distracted
by the increasing stick force and stick shake. Due to the lower rotor
RPM and subsequent much lower drag the aircraft accelerated much faster
than usual to a speed faster than the rotor would auto-rotate at the given
collective. Now without auto-rotation to drive it, the rotor continued
to slow down. The centrifugal force on the rotor continued to decrease
with the decrease in RPM, which resulted in more rotor coning, which,
in turn, caused the center of rotor drag to move up and away from the
spindle pivot. This increasing moment tried to tilt the rotor spindle
back, which Don had to resist with more stick force.
Don now realized his rotor RPM was low, but because of his concentration
at just flying the aircraft never realized his RPM had dropped as low
as 230 RPM or his airspeed had climbed to nearly 100 MPH (he learned this
later only after reviewing the recorded flight data). Don also did not
realize the excessive blade flapping and stick-force visual alarms had
been activated in the cockpit. Jay Shapley, riding as co-pilot, had been
temporarily distracted by cockpit management duties and was thus unprepared
to react to the sudden and totally unexpected turn of events. Had the
planned dual flight control system been installed, Jay would have been
able to provide some stick force help.
Don managed to take his hand off the stick long enough to reduce the
throttle and collective, but then increased the throttle again to keep
from hitting the ground at a pitched-up attitude of approximately 30 degrees.
At this attitude and 74 MPH, the wings were in a deep stall, which, in
turn, reversed aileron control. The rotor had slowed to 230 RPM - yet
the aircraft continued to fly. (In the post flight review of the data,
everyone was surprised that the aircraft continue to fly in this situation,
which was entirely outside the theoretical flight envelope. The aircraft
proved once again that it is very forgiving.)
Not knowing for sure what had happened, Don landed the aircraft as soon
as he got the aircraft leveled out. As the landing gear compressed to
absorb the vertical impact, the nose pitched over and Don instinctively
pulled back on the stick. The rotor acts like a gyroscope and will not
change its plane of rotation as fast as the aircraft can pitch over. Therefore,
when the aircraft pitched over, the rotor was pulled down toward the rudders.
This combination of the aircraft pitching over, the rotor being tilted
back more than 9 degrees due to the flapping caused by low RPM, and Don's
pulling back on the stick when the nose dropped - all contributed to the
rotor hitting the vertical tails, horizontal stabilator and prop. Almost
simultaneously with the rotor striking the rear of the aircraft, the nose
boom dug into the soft asphalt at the edge of the runway -- causing a
hard left yaw that almost rolled the aircraft to the right. The right
wing stopped the roll but was broken in the process.
Click on pictures to view
larger versions
LESSONS LEARNED AND PLANS FOR AVOIDING A RECURRENCE
Had the nose gear not compressed as far or had the rotor not been flapping
as much (due to low rotor RPM) or had Don pulled collective rather than
tilt the rotor back after landing - it is likely no damage would have
occurred.
A higher rotor RPM would have prevented the rotor from flapping as much.
Three changes will be made to help insure sufficient rotor RPM at this
stage of future flights. First, a large (additional) rotor RPM display
will be added to the top of the instrument panel. Next, a headset voice
alarm will be triggered automatically by the flapping sensor. The urgent
warning will state "Flapping over 5 degrees, reduce collective."
As a failsafe, the onboard computer that monitors 60-plus channels of
data will provide redundancy. The computer will trigger the voice alarm
when it calculates that rotor flapping is over 5 degrees based on collective
pitch, rotor RPM and forward speed.
Had the nose not dipped so dramatically on landing, Don would not have
reacted instinctively by pulling the stick back instead of pulling collective.
Also, the nose boom could not have dug into the ground at the edge of
the runway causing the aircraft to spin sideways and try to roll over.
Two changes will be made to assure the aircraft remains in a more level
attitude should a similar situation occur in the future. First, the nose
gear will be extended an additional six inches. It will also be redesign
to insure that the gear does not compress as much for a given load.
EXTENT OF DAMAGE
PARTS THAT APPEAR TO BE "OK": Fuselage and everything inside
-- including the cabin, the engine and the drive train. The rotor head
and the left wing are also OK. The landing gear appears to be undamaged
even though it absorbed a severe impact and skidded sideways down the
runway.
PARTS THAT ARE DAMAGED OR DESTOYED (see pictures): Rotor, prop tips,
right wing, both vertical tails & rudders, and the horizontal stabilator.
The rotor could be repaired since the carbon fiber spar appears to be
OK. However - it will be replaced since work had already begun on a new
generation, larger diameter rotor (see below).
Two inches of each prop tip are damaged, but otherwise the prop looks
fine. However - it will be replaced since work had already begun on a
new generation, slightly larger diameter prop (see below).
The right wing spar broke where it slides into the center section. It
will be repaired.
ADDITIONAL IMPROVEMENTS TO BE MADE
All of the improvements listed below were planned and in the process
of being implemented before the accident. They will be included in the
rebuild process.
- Finish installing dual controls
- Install our next generation rotor.The rotor diameter is increased
by 10-feet, from 33½ to 43½-feet. The new spar design requires less
force to change pitch. John Roncz designed the new airfoils.
- Change the drive ratio that will be used to pre-rotate the new, larger
diameter, slower turning rotor.
- Install our next generation prop. The prop diameter is increased by
2-inches, from 94 to 96-inches. The new prop design makes it easy to
build a four-bladed prop, which will be needed for future turbo-prop
engines. The new design will also incorporate a closer-fitting cuff
to a larger diameter spinner, which will reduce drag.
- Add more moveable rudder area.
- Add more horizontal stabilator area. 3-foot extensions will be added
outside of the tail booms and rudders. Studies show the additional surface
area may be needed at airspeeds above 200-MPH. This will also move the
aircraft aerodynamic center of lift rearward, allowing us to remove
some weight from the nose boom. The extensions will be removable so
the aircraft can continue to be transported by trailer.
- Eliminate the air-scoop on the bottom of the aircraft. The air will
be brought in from the top over the engine - then through the radiator,
the turbo inter-cooler & after-cooler and oil cooler before exiting
through a variable opening flap at the bottom rear of the aircraft.
This new design will work for both piston and turbo-prop engines.
OUR TWO WORSE FEARS
Our worst fear has always been that during flight testing someone would
get hurt (or worse) for any reason; whether it be a design deficiency,
structural failure, or human error. In this accident there were no structural
failures leading up to the accident and, in hindsight, there were very
human mistakes made by the pilots and the ground crew. Even though both
pilots feel that they were never in mortal danger, everyone involved still
feels fortunate no one was hurt. For this we are very thankful.
Our next worst fear was that the CarterCopter would be destroyed before
we had a chance to prove its concept. This would give the skeptics a chance
to say, "See, I told you they would never achieve their claims."
In this instance, damage to the aircraft could have been much worse. For
this we are also thankful. We also learned a lot about the aircraft. Under
the circumstances, it behaved better than expected. It seems to want to
fly, regardless of our mistakes. More than ever, everyone associated with
the project believes "we have a winner". The rebuilt CarterCopter
will be much improved. Estimated time required to be flying again is 4
to 6 months.
Although the planned flights for the stockholder meeting held on Sunday
December 19th did not occur, the unanimous decision among the stockholders
was that additional funding would be immediately made available and that
maximum effort be expended to expedite repairs and implementation of the
numerous improvements.
Image Gallery of Flight Incident
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