PRESS RELEASE, June 12, 2000
Wichita Falls, Texas: Monday, June 12, 2000
Edited by Rod Anderson
FLIGHT TESTING TO RESUME IN EARLY
JULY
We have been very busy the past several months trying to complete the
repairs, make improvements and do the proof testing. The repairs and improvements
took longer than hoped, but the proof testing on the wing, prop and rotor
head structure were completed with only a small void problem on the leading
edge (L.E.) of one prop blade. The new rotor system is completed and is
undergoing testing in the test pit (see status below). Between debugging
a new data-collection system for the test stand, chasing down some hard
to explain vibration frequencies, and adding L.E. weight to the rotor
blades to fix a blade weave, we lost a precious 3 weeks. We expect to
be flying approximately 3 weeks after the rotor tests are completed. Unfortunately,
insufficient time remains to do everything that is needed and still fly
to Oshkosh. We decided last year that we would not take the aircraft back
to Oshkosh until we could fly it there and show off.
NOTABLE BENCHMARKS FOR APRIL
- Completed the new 96" diameter prop, which weighs 10% less than
the previous prop (27 lbs. total, including hub, pitch horn and linkage).
- Completed the prop test program. Total of 12 minute run time @ Mach
0.63, 0.71, 0.79, 0.87, 0.95, & 0.99.
- Completed torque proof test on the rotor drive.
- Completed installation of co-pilot flight controls in the cockpit.
- Finished a design study of the CarterCopter Heliplane. The VTOL has
full hover capability and is similar in size, performance and cargo
capacity to the C-130 Hercules. A press release describing its features,
performance, and with drawings showing how it might look will be released
soon.
New prop static performance:
| Test Stand* Engine RPM |
Torque |
HP |
Prop RPM |
Tip Mach** |
Pounds Thrust |
| 4000 |
313 |
238 |
1676 |
0.63 |
1270 |
| 4500 |
313 |
268 |
1885 |
0.71 |
1400 |
| 5000 |
305 |
290 |
2095 |
0.79 |
1455 |
| 5500 |
294 |
307 |
2304 |
0.87 |
1440 |
| 6000 |
263 |
300 |
2514 |
0.95 |
1344 |
| 6250 |
236 |
280 |
2618 |
0.99 |
1120 |
*Drive ratio will be 2.75 for aircraft vs. 2.387 used
for test stand. Engine RPM is limited to 6500 maximum as set by the engine
computer.
**0.85 Mach is max resultant tip speed limit in-flight as set by the prop
computer.
NOTABLE BENCHMARKS FOR MAY
- Completed fabrication of the new rotor. The new rotor, hub and blade
pitch horn weigh 274 lbs., which includes129 lbs. of L.E. weight (inertia
& C.F.). The rotor is 43.5 ft dia. x 40.5 ft2 area. The original
rotor, hub and blade pitch horn weighed 240 lbs., which included 110
lbs. of L.E. weight. (33.5 ft dia. x 27.6 ft2 area).
- Selected 3 new pilots (see website
for resume)
- Moved the prop pitch computer and some data collection hardware from
behind the instrument panel to a more accessible location at the rear
of the cockpit.
- Completed 16,000-lbs. proof load test on the new rotor head (from
mast attachment to rotor spar).
- Completed 12,000-lbs. proof test on the rotor head mast attachment,
including an additional moment load of 7500 inch-lbs.
- Completed 4-g proof test on the repaired wing (based on a max gross
weight of 3000 lbs.).
- Filed additional patent improvements and new patents relating to the
CarterCopter Heliplane.
WORK REMAINING BEFORE NEXT FLIGHT
- Finish the rotor test.
- Remove the engine from the test stand and re-install it in the CarterCopter.
- Complete the installation of the new oil cooler, two new radiators
and the two air coolers for the low and high-pressure turbo (the turbo
will not be installed at this time).
- Complete the installation of all electrical systems (including the
voice alarms).
- Complete the installation of the variable-opening cooling air duct.
- Fabricate a new, larger diameter prop spinner.
STATUS OF ROTOR TESTS
The goal is to verify that the rotor system can operate smoothly to an
over-speed proof RPM of 465 (tip speed of Mach 0.95) without blade weave,
flutter or divergence. If 465 RPM is unattainable, the tests will go to
the maximum RPM possible at flat pitch with maximum HP available from
the engine. Maximum jump takeoff RPM is expected to be 425. The procedure
is to increase RPM by smaller increments at each increase in rotor RPM
speeds. At each RPM increment the rotor is excited with progressively
larger collective pitch jabs until collective is at its maximum or the
lift reaches 5000 lbs. If the loads are satisfactory and any oscillations
that occur dampen out quickly, then the tests proceed to the next higher
RPM level. Once the maximum RPM has been reached, the rpm will be lowered
to 425, the clutch disengaged, and the collective pulled as required to
first hold 3500 lbs. as long as possible (record the time), then 4000
lbs., 4500 lbs., and finally 5000 lbs.
During testing, the following information is recorded on a strip chart
recorder:
- blade pitch
- flapping
- blade pitch link load
- cyclic loads
- rotor RPM
- rotor lift
- collective stick force
- pylon movement fore & aft and side-to-side
At 375 RPM, the rotor experienced a blade weave, which did not fully
dampen out until the RPM dropped to 250 RPM, which took 7 seconds. The
new rotor was built with the same chordwise balance weight of 55 lbs.
(depleted uranium) per blade as used in the previous, shorter rotor. It
was calculated that by making the trailing edge lighter on the new blades
by using honeycomb and carbon prepreg, it might be possible to mass balance
the blades without additional L.E. weight. In the event additional weight
was needed however, the blades were fabricated with two hollow L.E. cavities
in which lead shot mixed with resin could be added. To resolve the blade
weave problem, the smaller outboard cavity on each blade was filled with
9 ½ lbs. of lead shot mix, bringing the total L.E. weight in each blade
to 64 ½ lbs.
We tried to increase the pylon dampening to reduce an oscillation that
occurred at 100 & 200 RPM. The change did more to increase the spring
rate than increase the dampening and made matters worse. To solve this
problem, so the rotor can operate continuously at any rpm, additional
instrumentation was installed. Several consultants were invited to observe
the tests and help analyze the data. During one of the following test
runs, the rotor head got into an oscillation that bent the cyclic control
rods (required a load greater than 2400 lbs.) and cracked the spindle
housing where the cyclic rods attach. We believe we understand what happened.
While a new spindle housing is being made, the pylon attachment to the
(very rigid steel) test stand will be modified to provide a lateral softness
more closely matching the aircraft. Also, the blade-teetering bearing
supports will be stiffened in the lateral direction. Further testing will
confirm if these changes solve the problem. There is always a certain
amount of trial and error with any new design, so the time factor for
completing the rotor tests is uncertain.
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