PRESS RELEASE, October 26, 2000
Wichita Falls, Texas: Thursday, October 26, 2000
Edited by Rod Anderson
CARTERCOPTER EASES INTO SOME BRIEF FLIGHTS
The CarterCopter (CC) returned to Olney, Texas, on Friday. October 6th
for resumption of flight tests. High-speed taxi runs were made Saturday
to explore the idea of doing a conventional autogyro rolling takeoff.
During one of these runs the aircraft lifted into the air approximately
one foot. The DV camera located on the tail recorded the event. The picture
quality of the DV camera and the recorded cockpit conversation are broadcast
quality and should provide the news media with exceptional materials in
future flights. The first goal is for the four new CC pilots to gain the
necessary flight experience using conservative procedures to protect both
the pilots and aircraft.
Fig. 1 - Short takeoff hop as seen by new tail camera
Note side covers removed during slow flight to help cooling.
The rolling takeoff idea presented several problems. We decided to initially
keep the rotor pitch constant to reduce the number of variables. When
the rotor was tilted back far enough to catch the air needed to maintain
the necessary rotor rpm, the CC would tilt back onto its training wheels,
which are designed for a max of 25 mph. We next tried tilting the rotor
forward to keep the training wheels off the ground until reaching (approx.)
50 mph -- at which time there was enough lift from the horizontal stab
to keep the tail up so the rotor could be tilted back. During the period
of acceleration to 50 mph, the rotor produced sufficient lift to raise
the CC up on its main gear but not enough to provide stability. Without
stability, cyclic control was very sluggish and rudder inputs caused the
CC to roll due to its (now extended) soft landing gear -- making the CC
feel unstable.
The pilots felt uncomfortable with the situation so it was decided to
change the takeoff procedure. They would try lifting off at a lower speed
by increasing collective. During the rotor over-speed run-up, the pilot
experimented with pulling collective to get its feel. The plan was to
limit the torque to 1800 ft-lbs for the initial tests but the torque display
was hard to see and he accidentally torqued the drive system to 2400 ft-lbs.
The gearbox failed. Later examination showed the ring gear support was
not stiff enough to keep the ring gear from pushing away from the pinion
gear, which moved its contact point out to the edge of the gear and greatly
increased its bending moment and stress level. This deflection aspect
had not been considered in the original design.
The following two weeks were spent designing, building, installing and
testing a modification to the gearbox ring gear support. The engine water
temperature got hot at Olney during low speed taxies, so we added another
fan to uniformly pull air through both radiators and the oil cooler. The
additional fan draws fresh air into the engine compartment and keeps it
cooler also.
DODGING RAIN STORMS
We returned to Olney Friday, October 20th and accomplished a few more
items on our checklists despite having to dodge rainstorms and fix minor
mechanical problems. The pilots decided to begin this flight-test program
by exploring hover type jump-takeoffs. We spun the rotor up 104 times
in the first 3 days of testing.
All day Friday and Saturday morning, we repeatedly over-speeded the rotor,
reduced throttle and pulled collective until the aircraft just cleared
the ground. There is a fair amount of stick friction/force so there was
a tendency to over control. This was uncomfortable for the pilots, so
the numerous repetitions were made in the hope the pilots would develop
a feel for controlling the aircraft.
The additional cooling fan worked fine, although after several rotor over-speeds
the engine needed to be idled for a couple of minutes to let the temperatures
drop. A few times we did not wait long enough and boiled the water.
Saturday afternoon was spent repairing the collective cable support located
inside the drive shaft going through the gearbox. The large number of
rotor prerotations overheated the gearbox, which in turn caused a bond
holding the collective anchor to pull loose. We drilled holes at the edge
of the tube and inserted roll pins to mechanically hold the collective
support.
For Sunday flight-tests, the pilots decided to let the aircraft roll forward
a little before pulling collective. They did this by releasing the brakes
and not reducing the throttle back to idle. They hoped it would give them
a little more time in the air before the rotor rpm dropped too low --
and possibly help reduce the lateral sensitivity. When they performed
this procedure, they found it made the lateral stability worst. As the
aircraft moved forward the downwash over the rear of the rotor increased
faster than at the front of the rotor. This caused an unbalance in lift
on the rotor and made the rotor plane of rotation dip to the right, which
had to be countered with a cyclic input to the left. The unbalance in
rotor lift changed with speed -- forcing them to constantly change the
cyclic input. Not having had any real experience at flying the aircraft,
and not knowing what to expect, the pilots were reluctant to climb up
more than a few feet or accelerate past 20 mph where the rotor control
should become easier. As a result we had a couple of hard landings (no
damage) that once again caused us to rethink the flight-testing approach.
RETURN TO THE ROLLING TAKEOFF
The following procedure was developed after consideration of everything
learned to date:
- Establish that the aircraft will not rock back on the training wheels
during acceleration if the rotor plane of rotation is kept parallel
with the ground.
- Establish the aircraft is stable and controllable at taxi speeds up
to 60 mph.
- Determine a throttle setting at the prerotate clutch release point
that can be held constant to provide the following:
- A comfortable acceleration whereby the rotor does not drop below
325 rpm by the time the aircraft reaches 30 mph.
- Sufficient HP to continue to accelerate in the relative high drag
of autorotation at the slow speed of 30-40 mph.
- Rapidly pull collective at 30 mph until the aircraft becomes airborne
and then continue to pull collective to hold the aircraft in the air
until the collective reaches a preset detent position of 5 degrees.
At this point the pitch cyclic will be varied to hold the desired flight
path.
- At 50-60 mph reduce the throttle to maintain airspeed or close it
entirely if the pilots become uncomfortable at any time with the way
the aircraft is handling.
During a rotor over-speed run up prior to completing the above procedure,
the gearbox again failed. The pilot did not add more torque than had already
been used numerous times before. The failure ended this second round of
flight-testing.
READY FOR ROUND THREE
We repaired the gearbox and will resume flight-testing this Friday, October
27th. We will pamper the gearbox by keeping the loads under 1500 ft-lbs
of torque. At 1500 ft-lbs we can still over-speed the rotor to 350 rpm,
which is sufficient to make short rolling takeoffs. Hopefully we can still
make a zero roll takeoff at this rpm once the proper technique is developed.
Failure of the gearbox delays flight- testing but is not dangerous to
the pilots since it is used only for prerotating the rotor prior to takeoffs
When we redesigned and rebuilt the gearbox ring gear support following
its first failure, we proof tested it by running it over 2600 ft-lbs of
torque for (approx.) 30 seconds and numerous additional times at over
2000 ft-lbs. The current gearbox problems are caused by the fact the gears
we are using were designed to turn in the opposite direction. We were
able to determine that our loads are trying to spread apart the gears
with forces 4½ times higher than normal due to the higher pressure angle
of the gear. During this week's repair, we increased the preload on the
tapered roller bearings to the maximum amount recommended. At the same
time, we reduced the backlash to the minimum amount recommended. If the
gearbox continues to fail, we will design and build another gearbox to
resolve the problem. This will take an additional 3-4 weeks.
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