PRESS RELEASE, November 20, 2000
Wichita Falls, Texas: Monday, November 20, 2000
Edited by Rod Anderson
Fig. 1 - View from wireless camera on top of rotor in
spinup during rotor testing
ONE NASA GOAL COMPLETED - FOUR TO GO
The four days from November 10th through the13th were our most successful
test period since the flight-test program began in September 1998. We
performed our first zero roll takeoff. This was the 1st of 5 goals set
for us by NASA under their SBIR Phase III grant program. We feel confident
that the CC rotor control problem with the new rotor head is solved and
that no major barriers remain to prevent us from completing the remaining
four NASA goals.
SOLVING THE ROTOR CONTROL PROBLEM
On Thursday, November 9th, we returned to the pit to test the most recent
control system modifications. They worked so well that we were able to
(1) eliminate the spindle stabilizer bar, (2) reduce the weight on the
spar stabilizer bar by 80% (may be able to eliminate completely) and (3)
disconnect the cyclic dampening. We limited the rpm to a maximum of 375
to keep from over-loading the pre-rotator gearbox any more than necessary.
At 375 rpm the rotor proved very stable even when the cyclic stick was
given a hard jab. The modifications also reduced cyclic stick forces by
more than one-half. The results of these tests indicated that the CC control
system would now respond similar to other rotorcraft the CC test pilots
had flown.
Friday morning we returned to Olney. By early afternoon we were making
test runs. Test pilots Rusty Nance, Dick DeGraw, and George Mitchell were
present. They confirmed almost immediately that eliminating the spindle
stabilizer bar had also eliminated any tendency for the spindle not to
follow the cyclic stick due to gyroscopic precession. With the cyclic
dampening disconnected, there was just enough stick shake to take a majority
of the friction out of the controls. This gave the pilots a better feel
of the flight controls. The pilots all agreed the stick forces had been
greatly improved.
Saturday morning was spent making a few minor changes. By early afternoon
the pilots were flying the full length of the runway for the first time
since we completed the CC rebuild program. There was still some yaw instability
(see below), but it was manageable. The pilots felt confident in their
ability to control the aircraft and began pulling collective to get airborne
at (approx) 30 mph -- resulting in several short takeoff runs.
SOLVING THE ENGINE COOLING PROBLEMS
Sunday morning was spent making a few changes to the air pressure system
and removing the cowl flap. We determined that a permanent solution to
the cooling would require the following changes:
- Create a vertical air-vent slot where the left and right sides of
the fuselage come together just below the prop. The new air-vent will
be 18 inches long and contain a clam shell cowl flap controlled by a
thermal switch to vary its width as needed from 4 inches to 10 inches.
- Remove the current air-exhaust fixture from the bottom of the fuselage
and fill in the hole with fiberglass.
- Extend the edges of the air inlet (on the front of the rotor mast)
forward by 8 inches. It will look similar to the air scoop found on
the bottom of a P-51 Mustang - only inverted.
SOLVING THE YAW INSTABILITY PROBLEM
By early Sunday afternoon we had determined the cause of the yaw instability
problem. The rudders were not aerodynamically stable about their pivot
axis. They were trying to align themselves at an angle of (approx) 15
degrees to the air stream - which caused the aircraft to yaw in the opposite
direction. When the pilots corrected for the yaw by applying opposite
rudder pedal, the rudders would snap to the 15-degree angle in the opposite
direction as soon as they crossed over the center. The back and forth
over-control caused a slow oscillation in an otherwise straight flight
down the runway.
The temporary fix was to adjust the rudder crossover control cable so
both rudders had their trailing edges pointed inward toward the aircraft
center line (approx) 15 degrees. This change put more of the rudder surface
area into the prop slipstream -- providing the additional benefit of improving
yaw control at low forward speeds. The permanent fix will be to move the
aerodynamic center of the rudders behind the pivot axis by adding 8 inches
to each rudder's trailing edge -and then rebalancing the rudders about
their pivot axis.
AT LONG LAST - THE FIRST ZERO-ROLL TAKEOFF
Following the temporary rudder fix, Rusty and Dick began progressively
increasing the throttle after releasing the rotor clutch and prior to
releasing the brakes - resulting in shorter rolling takeoffs. When they
finally reached full throttle before releasing the brakes, they accelerated
to 30 mph very quickly. Next, they began pulling collective at progressively
lower air speeds until they suddenly found themselves making the first
zero-roll takeoff for the CarterCopter. The digital video camera mounted
on the top of the right vertical stabilizer clearly recorded this historic
event along with the radio conversation.
Observers unfamiliar with the CC program would probably not be impressed
with this first success. Initially, the aircraft lifted vertically only
a few feet off the runway and never climbed higher than 10 -12 feet. To
everyone involved, however, the takeoff indicated the potential for some
very spectacular takeoffs in the near future. This time we were concerned
about overloading the pre-rotator gearbox and causing it to fail again.
We therefore over-speeded the rotor (prior to takeoff) to only 365 rpm
instead of the 425 rpm the rotor is designed for. Everything else was
also conservative. The pilots pulled just enough collective (6.8 degrees)
to clear the ground. They then reduced the collective as the aircraft
accelerated. This kept the rotor rpm and the stored energy (much less
than would be available with normal rotor over-speed of 425 rpm) as high
as possible until the pilots were sure they had reached 50 mph. They remained
close to the ground on purpose. Insufficient rotor energy (for any reason)
would simply have caused the CC to settle gently back to the runway. As
it happened, the rotor rpm dropped to only 285 rpm by the time they reached
50 mph. Rotor rpm at 5 degrees collective and 60 mph is 210, approx one-half
of the design takeoff rpm. Following this flight, the pilot's jump takeoff
confidence went up dramatically. The late hour caused this to be the final
flight of the day.
Fig. 1 - View from chase vehicle after zero roll takeoff
PRE-ROTATOR GEARBOX FAILS FOR THE FIFTH TIME
Monday morning we were able to start flying earlier than usual. The only
preflight change was an adjustment to reduce the rotor clutch disengagement
time. Since the first flight of the day had in the past always given us
the most problems, we decided to make at least 3 progressively shorter
rolling takeoffs before we started optimizing the jump takeoff procedure.
This was to make sure everyone was comfortable and back in the test groove.
For the 4th flight and the 1st jump takeoff of the day, we planned to
duplicate the previous day's success. After that the pilots would progressively
pull more collective on each successive takeoff and hold it longer --
causing the rotor rpm to drop to a more efficient rpm quicker. Recall
that rotor drag to the aircraft is a function of the rpm ratio cubed --
so slowing the rpm quickly does 2 good things; (1) the rotor energy is
much more efficiently converted to altitude -- which is desirable, and
(2) the drag is greatly reduced so the aircraft can accelerate to its
minimum HP condition much faster.
During the over-speed of the rotor prior to the start of the 4th flight,
the rotor had reached 340 of the planned 365 rpm when our pre-rotator
gearbox failed for the 5th time. It is now obvious that the gearbox is
overloaded, even at the reduced torque required for the lower pre-rotate
rpm's. At the time of this failure, everyone felt confident we were going
to perform several very impressive jump takeoffs before the end of the
day.
Fig. 2, 3 - View from rear after short takeoff on last day of testing
PREPARATIONS WELL UNDERWAY FOR THE NEXT FLIGHT-TESTS
The 8-inch rudder extensions necessary to solve the yaw instability problem
are almost complete. The engine air-inlet and air-exhaust alterations
necessary to prevent future ground cooling problems have been designed
and will be tackled next.
The preliminary pre-rotator gearbox design is completed and the required
helical bevel gears have been delivered. Based on specs received from
the gear manufacturer, we estimate these new gears will last 100 times
longer when using the same loads we used previously -- but their life
expectancy will decrease dramatically with increased loads. To compensate,
we will do a rotor confirmation test in the pit at 450 rpm (rotor tip
speed of mach .92) and then limit the number of max performance takeoffs
at the max takeoff rpm of 425 (for show). Most of the jump takeoffs will
be made at a lower rpm and pre-rotate torque in order to extend the gear
life. There was insufficient room in the present engine compartment configuration
to make the gearbox larger. We will not have this space problem when maximizing
the gearbox design for use on future CC prototypes.
There is a 50-50 chance of being ready to fly again by Friday, December
8th. The following weekend will be a better bet. Everything depends on
the weather and other factors that are beyond our control. We are anxious
to begin flight-testing again as soon as possible. The next NASA goal
we hope to achieve will be a zero-roll landing. Our pilots believe this
will be easier than the zero-roll takeoff, as they now feel very comfortable
with the aircraft's flying characteristics and the amount of energy that
can be stored in the rotor. Your interest in our R&D program is appreciated.
Please forward this press release to your friends.
Fig. 4 - Short takeoff from side view
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