PRESS RELEASE, December 21, 2000
Wichita Falls, Texas: Monday, December 21, 2000
Edited by Rod Anderson
First the Good News
A press conference and award presentation was held on Thursday, 14 December
2000 in Wichita Falls, Texas. The Popular Mechanics' Design and Engineering
2000 award was presented to CarterCopters, L.L.C. for the design of the
CarterCopter Heliplane Transport (CCH-T). PM's Editor-in-Chief, Joe Oldham,
presented the award. Jay Carter, Jr., president and principal engineer
/ inventor, accepted the award for CarterCopters.
The PM award was highlighted in the December 2000 issue of PM. The CCH-T
is considered by PM and many others to be the first significant new aircraft
design of the 21st century. According to PM the CC gyroplane / Heliplane
concept could reshape the face of aviation. PM is published in four languages
and sold in 11 countries.

(from left to right)
Jay Carter, Jr. - President
Joe Oldham - Editor-in-Chief of P.M.
TEAM MEMBERS
Stan Clines - Composites expert
Mark Robinson - Welder, mechanic,machinist
Brad Redding - CNC mill programmer, machinist
Loi Tran - Electrical engineer, website, computers
Shane Teeter - CNC lathe programmer, machinist
Troy Tally - AutoCad draftsman
More Good News
Flight-testing of the CC prototype resumed at Olney on Wednesday, 13
December (the day before the PM award presentation). The pilots made 12
flights down the runway. During the takeoff and climb portion of each
flight the pilots' effort was directed towards understanding how best
to use the stored energy in its rotor. They also wanted to see how quickly
rotor rpm would increase during flight once the collective was reduced.
Both pilots were delighted with the results. The first few landing sequences
were used to confirm the ease of performing zero-power landings with the
incredible amount of rotor inertia available. The pilots were more excited
than ever before about the aircraft's responsiveness and the obvious potential
for performing zero-roll landings (the 2nd of NASA's 5 goals). They felt
the first zero-roll landing would come before the end of the day. They
commented that the prototype flew so smoothly they could not tell by feel
that they were flying in a rotary wing aircraft. They compared the sensation
to flying in a sailplane in smooth air. There was a complete lack of rotorcraft-type
vibrations or shake of any kind. This perception of smoothness included
the controls. There was absolutely no stick shake. This is very unusual
-- especially in a direct control rotorcraft with no boost.

Aircraft ready to taxi during November testing &
fly-by during December 13th, 2000 testing.
Bad News: Non-event Causes Major Damage
At the conclusion of the 12th flight, the totally unexpected happened
again. The CC slowly ran off the end of the runway at 20 MPH. In the span
of just a few seconds, the non-event landing suddenly turned into a nightmare.
The damage to the aircraft can be repaired in 3-4 weeks. It will take
2-3 months to build, balance, & install a new rotor and then proof-test
everything in the test-pit.

Aircraft after pulling nose boom out of ground.
The CC landed gently at 30 MPH with plenty of runway remaining. For reasons
unknown to the pilots at the time, the brakes were not effective. One
pilot later commented that the only options he could see were to swerve
sharply left to the taxiway and risk blowing a tire and dragging a wing
or hope the overrun was firm enough and speed slow enough to support the
aircraft. The result was -- it wasn't. It was a tough, spit-second judgment
call that went the wrong way.

Blades broke at hub with minimal damage to hub & rotor head.
Blade spar will handle 500,000 lbs. of centrifugal force but will
break off at the hub on both blades if one blade hits the ground solidly.
Rolling slowly off the runway at 20 MPH would have been a non-event as
the pilots hoped except for the fact the ground was very soft from recent
rains. As a result, the front landing gear sank to its axle. The intense
drag this created caused the (long) front landing gear to fold back as
though it was retracting. Even with the gear folded back the incident
would have remained a non-event except for the 4 feet long nose boom (part
of the ballistic chute system) that speared the ground with the 3,000
lb aircraft pushing. The sudden stop from 20 MPH caused the CC to pitch
over on its nose to a near vertical position -- allowing the rotor to
strike the ground. The aircraft looked like it might remain in the vertical
position like a dart stuck to a dartboard (quite a sight), but after a
brief hesitation it rolled onto its right wing. The wing prevented the
aircraft from rolling further. After a few more breathless moments the
aircraft finally fell back onto its landing gear.

Top of rudders chopped off when aircraft nosed over.
Booms were undamaged.
If the nose gear had not folded under -- the nose boom could not have
speared the ground and nothing serious would have happened. The nose gear
had folded under during the December 1999 accident with similar results.
That time it had folded due to the forward pitching moment cause by the
hard landing and the brakes being applied hard. To prevent the same thing
happening again an excess amount of oil was added to the front gear. This
caused the front gear to bottom out before it could compress enough to
allow the nose boom to (again) dig into the ground. Every time the gear
is retracted (either fully or partially) the current oil-air separator
permits a fine mist of oil to escape into the air. The oil is automatically
replaced from a reservoir each time the gear is fully cycled in
flight. During each of the numerous trips to and from the pit to proof-test
the rotor and gearbox, we had to partially retract the front gear to clear
the top of the door opening at the CC shop. Apparently enough oil escaped
into the air from these numerous retractions to let the nose gear compress
too far -- again. During our subsequent flight-testing, the flights down
the runway were too brief for the pilots to retract the gear which would
have automatically replaced the escaped oil.

Blade 30 ft. from aircraft. Tip came off when
the blade first hit the ground.
Damage to the CC prototype includes the following: (1) the rotor was
destroyed, (2) the rotor mast was damaged, (3) both rudders were clipped
off near the top by the rotor, (4) the right wing was broken about 5 ft
from the tip and (5) several parts of the rotor head and prerotator drive
will need to be replaced. The reinforcement we added to the rear wing
spar attachment after the December 1999 accident kept the wing from failing
again at the root.

End of outboard 7 ft. of 2nd blade buried in ground.
Brake Mystery & Solution
When the pilots emerged from the aircraft they both thought the brakes
had failed. The aircraft had not slowed down when they pushed hard on
the brake pedals. Until this landing the brakes had worked without any
problems. They appeared to work fine when the aircraft was rolled back
onto the runway.
Looking at the data transmitted from the CC during flight-tests solved
the mystery. Once reaching 400 ft altitude the pilots had progressively
lowered the collective a little more than they did the previous flight.
This allowed the rotor to speed up before they started the landing flare.
The pilots were surprised at how slowly the rpm dropped as collective
was pulled to keep the aircraft in the air -- and how far they were able
to float down the runway. As they got closer to the end of the runway,
they decided to let the aircraft settle onto the runway by not pulling
any more collective. At this point the rotor rpm was 180, the airspeed
30 mph and the collective 8.5 degrees. At touch down, the pilots were
discussing the beautiful flight and the energy remaining in the rotor.
Collective was inadvertently not lowered before applying the brakes and
with the rotor still providing a lot of lift, the wheels just slid lightly
down the runway without providing the needed braking action.
An alternative braking solution (beside the brakes) was available but
was not used soon enough. The rotor on any gyroplane can be tilted back
to provide a rotor brake during the landing procedure. The method was
used in this case but only after rotor rpm and lift had dropped off --
permitting the brakes to become more effective. The aircraft is normally
tilted forward 3.5 degrees, so the rotor has to be tilted back 3.5 degrees
just to be level with the runway. To provide enough rotor tilt to be effective
at stopping the aircraft, the CC must be rocked backwards onto its tail
boom training wheels. In this case it was not tilted back far enough or
soon enough to overcome the forward pitching moment of the brakes.
Probable Reasons
The question was why the collective had not been lowered after touch
down. This is standard procedure that had been followed previously without
fail. The most likely answer is that the pilots were distracted (excited)
as to how much energy was in the rotor and how long they were able to
keep the aircraft in the air. The collective itself could have been a
contributing factor. It has a spring that toggles over center at approximately
3 degrees of collective. As the spring toggles over center it applies
a force to help the pilot pull more collective easier. This is necessary
because the high centrifugal force on the blades caused by the 65 lbs
of rotor-tip weights per blade provides a moment to keep the blade pitch
in the rotor plane of rotation. The pilot has to overcome this moment
in order to change the blade pitch. For any given pitch this moment will
increase or decrease as a function of rpm squared. This means that by
the time the rotor rpm has dropped to 180 rpm, the collective force at
8.5 degrees is negative -- requiring the pilot to now push the collective
down to reduce pitch instead of having to hold it up. Collective force
was therefore not available to remind the pilot to lower the collective
after landing (as would be on most other rotorcraft).
Steps Taken to Prevent a Third Reoccurrence
This is the second time the aircraft has suffered major damage as a result
of the nose boom digging into the ground after the nose gear compressed
(the December 1999 accident was the first). In this case if the nose boom
had not dug into the ground, the nose of the aircraft would have slid
across the ground and little if any damage would have been done. To prevent
the possibility of this happening a third time, the boom will be shortened
so it cannot dig into the ground.
A new oil-air separator has been designed for the nose gear that prevents
any oil from escaping when the gear is retracted. This should prevent
the nose gear from being able to compress and fold under due to a shortage
of oil -- should a similar emergency occur in the future.
A Pilot Operating Handbook (POH) for the CC gyroplane has been under development
for some time by our pilots. Now they intend to include a new section
on fast stop procedures while taxiing. An effort will be made to brainstorm
as many other emergency scenarios as possible and work out the best procedures
in advance. At some point in the future when finances permit, the ideal
solution might be to develop a CarterCopter flight simulator and incorporate
these scenarios for training purposes.
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