PRESS RELEASE
Wichita Falls, Texas: Friday, 10 August 2001
By Jeff Keaton. Edited by Jay Carter, Jr.
Spinner Bracket Failure Causes Emergency Landing
On Sunday, August 5, 2001 while flight-testing near Olney, Texas, Rusty
Nance, Chief Test Pilot of the CarterCopter Technology Demonstrator (CCTD),
made an emergency landing after the bracket that holds the propeller spinner
failed. Larry Neal was also on board at the time serving as Copilot and
Flight Test Engineer. The CCTD was at an altitude of 4000 feet MSL and
accelerating through 125 mph when the spinner support bracket failed,
causing a loud bang and severe vibration. The spinner quickly disintegrated
and its pieces impacted other parts of the aircraft including the tail
booms, propeller, rotor, and cowl flap. The pilots immediately shut down
the engine and executed a successful, very low speed dead stick landing
on the runway. There were no injuries to the pilots or anyone on the ground.
In three years of flight-testing, this is the first in-flight mechanical
failure not associated with the powerplant and the second emergency landing.
This incident demonstrates some of the safety features designed into
the CarterCopter. Because its ratio of lift to drag is better than any
other rotary wing aircraft, it had plenty of range to easily glide back
to the airport. The pilot was then able to transition to autogyro mode
and make a very low speed, short landing.
This event ended the flight-test series that began on Friday, August
3 to evaluate a configuration change which moved the rotor aft in order
to reduce the amount the aircraft would be pitched up at lower airspeeds.
Another recent modification to prevent the landing gear from collapsing
all the way if the air pressurization system failed, involved increasing
the amount of oil in the landing gear system when extended. An engine-driven
air compressor provides the principal air pressurization and pressurizes
the system in less than 20 seconds. The backup electric compressor takes
approximately 8 minutes to fully charge the landing gear and is also used
as a backup to the control force trim system. With the engine shut off,
there was not enough time to fully pressurize the landing gear. The extra
oil in the landing gear kept the landing gear from fully retracting and
prevented any additional damage from occurring during the forced landing.
Initial failure analysis indicates a fatigue failure in the spinner bracket
caused by stress concentrations in a non-tempered welded joint. This steel
part had been in use for approximately 200 hours. We normally stress relieve
welded parts, but did not on this part. The new spinner support bracket
will be heat-treated, tempered, and built from material with three times
the tensile strength of the old bracket. The propeller will have to be
rebuilt, but we may be able to reuse the spar which would save 3-4 days
of work. Repairs and modifications will take four to six weeks before
flight-testing can resume.
Spinner failure sequence 5 August 2001
In addition to making repairs, we plan to make two modifications. We
will change the rotor teetering axis angle (delta 3) from 30º to 10º which
will allow the rotor to track the spindle movement exactly and not momentarily
move some 90º to the direction of the spindle travel. In order to go faster
than 160 mph, we will also rework the aft section of the aircraft fuselage
to reduce the amount of air separation. This separation is significant
and could cause an equivalent several square feet of flat plate drag.
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