PRESS RELEASE
Wichita Falls, Texas: Friday, 5 October 2001
By Jeff Keaton. Edited by Jay Carter, Jr.
Failure of Modified Propeller Leads to Design Improvement
In preparation for flight-testing scheduled September 21, 2001, the CarterCopter
Technology Demonstrator (CCTD) suffered significant damage during a qualification
proof test on a modified propeller in the "pit." The propeller
-- which had been newly constructed as a result of damage that occurred
August 5, 2001 abruptly failed, resulting in damage to the tail
boom, composite landing gear support, fuselage, and numerous metal parts.
The prop drive shaft was bent so badly that the pre-rotator pulley tried
to engage the rotor drive with enough torque to break the main U-joint
at the rotor head (which had been previously proof tested to 3000 foot-pounds).
The prop failed at an engine RPM of 4000 during a full throttle acceleration.
In prior tests, the prop had run up to an engine RPM of 5750. Since the
rotor was not turning and the prop spinner was not installed, these parts
were not damaged.
The propeller spar was fabricated using KEVLAR® instead of
carbon fiber because KEVLAR® is tougher and less brittle than
carbon. The KEVLAR® was compared against carbon in side-by-side
tests for tensile and shear strength with similar performance. There was
a potential risk in buckling due to the fact that KEVLAR® has
about 2/3 the stiffness of carbon -- but since most of the loads would
be in tension this was not expected to be a problem. However, a full throttle
acceleration (maximum torque, but reduced centrifugal force due to the
lower RPM) with the prop at flat pitch (spar twisted the maximum amount),
caused the spar to buckle. The spar did not fail in tension due to centrifugal
force or in shear due to a bond failure.
Required repairs include making a new prop, fixing the composite fuselage
and landing gear support, machining 17 aluminum and steel parts, and repairing
the starboard tail boom that was nearly severed by one of the prop blades.
Prop failure sequence at 30 frames per second -- 18 September
2001
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| 1/30 sec. Prop spar is starting to fail |
2/30 sec. |
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| 3/30 sec. 1 blade has departed. 1 blade is cutting
tail boom |
4/30 sec. Prop shaft is severely bent |
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| 5/30 sec. |
6/30 sec. Note tumbling blade in background |
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| 7/30 sec. Note top antenna movement |
8/30 sec. Piece of KEVLAR® spar in foreground |
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| 9/30 sec. |
10/30 sec. Note upper cowling distortion |
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| 11/30 sec. |
12/30 sec. |
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| 13/30 sec. Rotor moved aft from applied torque |
14/30 sec. |
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| 15/30 sec. |
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The failure of the KEVLAR® spar suggests that although the
carbon spar never failed, it was marginal. This test highlighted a
potential problem that could have eventually occurred in flight at
high altitude and very high speed -- the only flight regime with a combination
of low prop RPM, maximum pitch/spar twist, and high engine power/torque.
Test Results and Other Design Enhancements
Some useful test data was obtained prior to the prop failure. For a given
constant high horsepower setting, static prop thrust was better at higher
RPMs which indicates the prop RPM needs to be increased to more efficiently
handle higher engine horsepower. A higher RPM reduces the prop angle of
attack and amount of blade stall. This also explains why the aircraft
performed better at higher engine/prop RPMs. The ratio of engine-to-propeller
RPM will be changed from 2.75:1 to 2.387:1. This should improve static
thrust, climb performance, and in-flight prop efficiency at higher power
settings -- and increase the centrifugal force for a given torque to help
stabilize the spar and avoid a buckling problem (centrifugal force is
a squared function of RPM).
Test data also indicates that the revised prop controller algorithm is
working well.
A new propeller has since been rebuilt, but the new prop spar was constructed
out of carbon with the addition of a carbon shear web to greatly improve
the column (buckling) strength. The spar winding process was also improved,
which increased the carbon content by 5% and provided better wet-out of
the strands. This new prop will be tested on the steel test stand rather
than on the aircraft to limit exposure to the aircraft.
Additionally, for added protection both tail booms will be reinforced
with KEVLAR® armor in line with the propeller plane of rotation.
All enhancements and repairs are progressing on schedule and flight-testing
is scheduled to resume in mid October.
Events of September 11, 2001 Force Pilot Changes
In support of recent military preparations, Rusty Nance will not be available
to serve as Chief Test Pilot for the next series of flight-tests. Larry
Neal, who has been flying with Rusty as copilot, will move into the left
seat and be the pilot. Professional test pilot Tom Currie will fly as
Principal Copilot and Flight Test Engineer with Paul Smith and Carl Hawkins
as backups.
KEVLAR® is a Dupont registered trademark.
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