PRESS RELEASE
Wichita Falls, Texas: Wednesday, 21 November 2001
By Jeff Keaton. Edited by Jay Carter, Jr. and Kenneth Hibbs
FLIGHT-TESTING STATUS UPDATE
New Flight Crew Training
During the last two weeks of flight-testing the CarterCopter Technology
Demonstrator (CCTD), the new team of Larry Neal (pilot) and Brad King
(co-pilot) has progressed from high speed taxi runs, to low altitude flights
down the runway - to flying the traffic pattern and making smooth takeoffs
and landings. Rusty Nance was able to attend for three days and his instruction
greatly accelerated Larry and Brad's learning process, although minor
problems with the aircraft shortened Rusty's time as instructor. Although
frustrating at times, debugging these problems after a major repair was
a significant accomplishment. Improved configuration control and flight
record documentation facilitated pilot training and corporate learning
-- preventing mistakes that have slowed flight-testing in the past.
New copilot Brad King
Repairs and Modifications
The CCTD was repaired after damage that occurred September 18, 2001 (see
Previous Press Release) when a newly constructed
propeller (made with a KEVLAR® spar instead of carbon) failed
during testing in the "pit." Repairs included: a new carbon
spar prop with a newly added carbon shear web, a new spinner with a new
heat-treated support bracket, repairing the starboard tail boom, machining
17 new aluminum and steel parts, repairing the rotor blade and fuselage
damage, and repairing and calibrating several sensors for telemetry data.
Other modifications were made during this period, including: changing
the collective range (From: 0° to 12°, To: -2° to 10°), adding a 0° collective
detent, installing new cyclic control cables with a more direct routing
to the rotor linkage, streamlining the aft lower section of the fuselage
and associated cooling air exhaust, designing and manufacturing a new
rotor hub and pitch horns to change the rotor delta three from 30° to
10°, changing the prop RPM controller algorithm, adding 4 layers of KEVLAR®
armor around both tail booms in line with the prop plane of rotation,
changing the ratio of engine-to-propeller RPM from 2.75:1 to 2.387:1,
and replacing the collective cable in the cockpit.
Old aft fuselage with cowl flap
New streamlined aft fuselage (no cowl flap)
Flight-testing October 26 to October 28, 2001
In order to train the new flight crew, the pilots first practiced procedures
in the flight simulator. With the help of the Golden Arms Associates,
detailed flight test records and data were analyzed and used to modify
procedures and checklists that the new pilots studied and practiced before
attempting to fly the CCTD. Then several high-speed taxi runs were made
in the CCTD that allowed the pilot to practice pulling collective and
capturing pitch in preparation for takeoff. During this period, flight
time was sometimes interrupted by small problems. This has come to be
expected after major repairs that require the removal and reinstallation
of numerous components. Although most problems were found during static
testing in the "pit," some problems didn't show up until taxi
tests - including loose connections, failed switches, brake cylinder leaks,
sensor malfunctions, bad circuit breakers, and coolant leaks. Even though
outside air temperature was around 70° F, the engine would occasionally
overheat during periods of repeated pre-rotations and taxiing.
At the completion of the first high-speed taxi run on Sunday, October
28, 2001, the aircraft was stopped using normal aerodynamic braking. After
the aircraft had stopped, the cyclic was inadvertently positioned full
aft with the collective at 9.5°. This control position, combined with
a headwind and low rotor RPM (approximately 100), resulted in excessive
rotor flapping which caused the rotor blade to hit and damage the top
portion of the both rudders.
Damage to rudders
Flight-testing November 8 to November 15, 2001
After repairing the rudders, flight-testing resumed on November 8 in
Olney. Changes were made in order to prevent a future rudder strike. A
voice alarm was added to warn when the sum of aft spindle tilt plus flapping
is too high. A mechanical stop was also added to limit aft movement of
the cyclic to 10°. Flight operations procedures were changed for the co-pilot
to more closely monitor flapping and rotor RPM and call out values to
the pilot more frequently. This situational awareness feedback is most
important when the pilot's workload is high, for example when learning
new flight procedures or being distracted.
Rusty Nance, who was only available for three days, began the flight
tests in the left (pilot) seat. After a few high-speed taxi runs to refresh
his feel for the aircraft, he flew five low-altitude flights down the
runway. During these short flights, a small vibration in the cockpit and
a stick oscillation were noted. Rotor balance and tracking were adjusted
to minimize these problems.
Rusty then traded seats with Larry, who practiced eleven high-speed taxi
runs before flying four low-level flights down the runway. Larry was able
to reach this competency level in a tenth of the time that it had previously
taken new pilots to learn to fly the aircraft for a few reasons. An experienced
pilot was in the right seat providing real-time instruction. Flight operations
procedures are now well defined and documented. Training for takeoffs
utilizes a build-up approach where more familiar procedures (similar to
autogyros or fixed wing aircraft) are used before more aggressively pulling
collective to shorten takeoff rolls.
Problems with the aircraft continued to interrupt flight-testing. A serpentine
belt came loose due to the failure of the air pump bracket. This belt
also drives the water pump and alternators. Overnight, the bracket was
redesigned and repaired.
The next day a few more low-level flights were conducted. The engine
tended to overheat with repeated rotor pre-rotations and slow speed, full
throttle flights. A water mist spray cooling system was added to the aircraft
and provided some improvement.
Three traffic pattern flights were then made; the longest was for 9 minutes
at 1000 ft AGL. The aircraft reached an airspeed of 117 mph with the rotor
slowing to 190 RPM. The rotor was unloaded to a point where the wings
were providing over 85% of the lift (500 lbs. on the rotor and 3000 lbs.
on the wing). This data is encouraging because it indicates that recent
changes in trim (relationship between the horizontal stabilator and spindle
angle) will unload the rotor and allow rotor RPM to decrease with increased
airspeed as designed -- and still keep flapping to a minimum. As rotor
RPM drops, the aircraft accelerates. Trimmed for a target airspeed of
100 MPH with constant throttle, the airspeed quickly reached 117 MPH as
the rotor RPM decreased. A speed increase was expected, but the amount
of increased airspeed still surprised the pilots.
Engine overheating continued to be a problem, so overnight more misting
nozzles were added to increase the injection rate of cooling water. However,
two days of bad weather (high wind, then rain) prevented further flight
tests. Additionally, while diagnosing an erratic reading on one sensor,
it was discovered that the main ribbon cable that interconnects all the
aircraft computers was worn out and intermittent. The aircraft was returned
to the shop to build and install a new cable.
Flight-testing is scheduled to resume in late November. Before then,
the rotor will be rebalanced and tracking will be adjusted to minimize
a one-per-revolution "cabin bounce" reported by the pilots.
The air intake area will be increased 80% and the air exit increased by
20% to improve engine cooling.
|