PRESS RELEASE
6 October 2003, Wichita Falls, Texas
We apologize for the
length of time since the last update. We have been very focused on repairing
the aircraft and getting it ready for flight testing. We will try to make
future updates more routinely.
CarterCopter Rebuilding Update
It has been almost
6 months since the CCTD suffered significant damage in a wheels-up landing
on 8 April, 2003. The interrupted flight test program to break the Mu
1 barrier will resume shortly with hopeful expectations. A special thank
you goes to the many donors to the OSAC Mu 1 club. Their generous donations
provide emotional and financial support as well as welcome reaffirmation
of our efforts. Anyone still interested in contributing is very welcome.
We will proudly write the names of all donors on the aircraft.

Repaired CCTD
During the rebuilding
program, we incorporated improvements that took much longer than expected
(mapping the turbocharged engine is one painful example) and added some
improvements to the project (total overhaul of the data collection wiring).
Many of the known weaknesses of the aircraft were corrected (landing gear
retraction system, communication system) and we believe we are in good
shape to proceed. The following list details the tasks accomplished in
the past 5 ½ months.
Airframe repair:
Repaired the co-pilot rudder, both tail booms where they attached to the
wing, the rotor, the upper rear fuselage and its attachment points. Made
a new shaped lower rear fuselage section to decrease air-flow separation
and decrease the drag. Made a new fiberglass cross-over beam to support
the prop bearing , a new prop drive shaft and bearing support, 2 herringbone
prop drive pulleys, belt idler, engine support plates, prop collective
shaft and hydraulic actuator, 2 belt accessory drives with dual redundant
water pump drive, and a new propeller same design as before.
New Engine:
Installed a new turbocharged 427 cu in Bow Tie LS 6 engine. This engine
uses the C5-R block with the best racing components and special CNC ported
heads. It should produce 400hp reliably and deliver 600hp for short periods.
The turbo is sized to maintain 42 inches of boost up to 20,000 ft. Also
added turbo cooler and auto controlled waste gate. Increased the size
of both the turbo oil suction pump (1.6 times) and the hydraulic boost
pump (2.3 times). Incorporated a 10 micron high pressure filter on the
boost pump. Mapping this turbocharged engine was a major obstacle since
we had great difficulty finding an available knowledgeable expert willing
to work on an aircraft application. This engine is used routinely in the
same configuration in racing cars. The belt idler force had to be increased
to handle the higher torque. A second reason for increasing the belt idler
force is that the quieter herringbone belt drive has a rounded tooth profile
which has more of a tendency to push the belt away from the pulley under
load.

New Engine & Turbo Being Installed
Aircraft Control
Systems: Modified the cyclic boost control so that if boost pressure
is lost when the rotor is at a very high mu and unstable, the irreversibility
feature is maintained long enough for the rotor to speed up to a stable
rpm. Tests will determine just how long the irreversibility will last.
The cyclic boost has also been set up so that the boost pressure can be
turned on and off to permit us to test how the cyclic functions in flight
without boost. The cyclic spool valves were modified so that there is
about .009 of dead band before the valve starts to open. For the last
flight the spool valves had been modified for zero dead band. With zero
dead band, there was excessive leakage and there was no irreversible feature
possible. Collective in manual mode has been changed so that the pilot
has to push on the button on the end of the collective and then apply
approximately 20# (adjustable) force to move the collective. The collective
will then move at a slow, but mechanically adjustable rate. If the pilot
applies approximately 40# of force, the collective will move at its fastest
rate. There are 3 new switches added to a separate switch panel located
on the end of the collective. The left switch of the three is a kill switch
for some of the new auto controls (flapping, rotor rpm, and pylon position).
It does not kill the prop auto pitch/rpm control or the waste gate control.
The center switch is a momentary type switch that controls the up and
down movement of the collective. Pushing or tapping the switch forward
moves the stick down and pulling or tapping it aft moves the stick up.
Tapping moves the collective slowly and will be used for a fine trim control.
Any time the collective is operated, either with the center switch or
by pulling/pushing the stick or by the controller in auto mode, both the
air and hydraulic boost are activated. If either the air or hydraulic
boost were lost, the other system could still move the collective without
the pilot first having to determine which system failed. The right switch
on the collective switch panel is a momentary switch that turns on the
engine cooling water spray. Pulling the switch aft turns the spray on.
Landing Gear:
The landing gear extension and retraction system was unnecessarily complex
and unreliable. This was one of the reasons it was not used frequently
during the flight-testing. An entirely new and much simpler landing gear
extension and retraction system was installed. This system uses a special
oil gear pump, which is basically 3 pumps in one, one for each of the
three landing gear legs. The pump transfers the oil from one side of the
landing gear cylinder to the other to cause the gear to extend or retract.
This eliminates the need for a lot of compressed air and about 15 solenoids,
several accumulators and an oil / air separator. The air in the top of
the cylinder creates the spring action. This air is captured and does
not need to be replaced unless there is a leak. The new design should
be much more reliable than the last design but we did have to be creative
with the gear motors. We were not able to find an off-the-shelf 12 v motor
the size and hp needed. We had to use a 24 v motor with relays to convert
2 batteries back and forth between a 24 v system for operating the motor
and a 12 v system so the batteries can be charged.

New Landing Gear Being Bench Tested
The Fuel System:
The fuel system still has 2 separate fuel pumps and filters, but we now
use 2 larger high pressure pumps that do not require a separate low pressure
pump to first suck the fuel out of the tank. The fuel system now has a
fuel flow meter so we can determine engine efficiency (BSFC) and aircraft
efficiency (MPG). The fuel system is simplified in that there is now only
1 fuel line to the engine instead of 2.
Electronics and
Wiring: The communication radios and hot mic set up were rebuilt.
New cables, connections, ground plane and antenna are expected to improve
reliability and quality dramatically. Over the years, the sensor system
had accumulated numerous additions and deletions, many of them poorly
documented. We believe that the required data set is now understood so
all unnecessary wiring was removed. All the sensors have been rewired
with shielded cables and connected to a common ground. The computers are
now tied together in a more direct fashion and considerable effort has
been made to reduce the electrical noise getting into the system. The
rewired system is now much more likely to remain calibrated and we expect
a large amount of reproducible data from the upcoming flight test series.
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