Proof Test Results
We have run the following proof tests on portions of the airframe:
Landing Gear Attachment proof test - the landing gear was installed in
the booms, the fuselage mounted to the floor such that it could not move,
and the landing gear pressurized with a hydraulic pump. The purpose was
to test the aluminum mounting points bonded into the fuselage and booms.
The nose gear was loaded with 5000 pounds and completed the test. The
main landing gear was to be loaded with 9000 pounds per wheel and the
mounting points began to fail at 6000 pounds. Therefore, the test was
halted until repairs and reinforcement could be made. Improvements were
completed, the test was redone, and passed. The attachments were also
improved to prevent galvanic corrosion between the aluminum bosses and
the carbon structure.
Wing Bend proof test - The wing was installed in the fuselage and bend
tested to 4 Gs. At 2.25 Gs a small area of the top skin initially showed
signs of buckling failure. The area was cut open for inspection and it
turned out the carbon cloth in that area was too dry and did not bond
to the foam sandwich. This area was reinforced and the test was successfully
completed to 4 Gs. The wing was retested after the landing gear attachment
proof tests to assure there was no damage.
Fuselage pressure test - the fuselage pressure vessel was completely
filled with approximately 6000 pounds of water, then pressurized to over
24 PSI (26 PSI at the fuselage bottom). Initially, the fuselage pressurized
door leaked due to slippage of the fuselage/door engagement mechanism.
By installing cam engagements locking the door and the fuselage together
(as was always planned for the final aircraft), this problem was solved
and the fuselage completed the test. The maximum flight pressurization
will be 10 PSI. The fuselage/wing fairing attached to the pressure vessel
came unbonded during the pressure test due to the stretching of the pressure
vessel, but this has now been fixed.
Propeller Tests - the version 3.1 prop was tested and failed at 6000
engine RPM. It was determined that the failure was caused by missing layers
of unidirectional carbon in one of the propeller skins (a quality control
problem not a design problem). The failure caused substantial damage to
the test stand but this provided an opportunity to improve the design
of the components that needed to be remade. Takeoff RPM in the actual
aircraft is expected to be 5500 RPM, but the propeller will be tested
rigorously at overspeed conditions on the ground to verify the desired
safety margins.
Propeller Tests - the version 3.2 prop was tested and failed at 6500
engine RPM (with the tip travelling at Mach .982). This failure was determined
to be due to a combination of blade weave due to the the high tip speed,
softness in the pitch linkage, and pitch links weakened to provide clearance
to set the pitch low enough to achieve a very high RPM. The test stand
was again damaged but not nearly as extensively as in the version 3.1
propeller tests. Propeller 3.3 is now being built with an improved pitch
link design which increased stiffness by an order of magnitude and allows
the pitch to be reduced without reducing the strength of the system.
Propeller Tests - the version 3.3 prop was tested and failed at 6550
engine RPM. The failure was determined to be because of tip delamination
due to failure of the bond between the skins and the foam core. The foam
had been substituted for flexibilized epoxy to reduce the weight in the
trailing edge of the blades in an effort to reduce the blade weave tendency.
As it turned out, the increased pitch link stiffness reduces the blade
weave loads to almost zero. The next prop will have solid resin at the
tip and an improved counterweight arm design.
Propeller Tests - the version 3.4 prop was tested to 6000 engine RPM
and passed. Actual operations will be limited to 5500 RPM (2300 prop RPM).
The prop has now been run for several hours at various RPMs with no problems.
The test procedure for all prop tests since version 2.1 was to run at
engine RPMs of 4500, 5000, 5500, 5750, 6000, 6250, and 6500 (tip mach
1.0). At each RPM the prop was run for four 15-second increments, then
four 30-second increments, then four 1-minute increments, the three 2-minute
increments with inspections of the prop and test stand after each run
before progressing to the next RPM level. A high speed stripchart recorder
was used to analyze the pitch link data.
Rotor Head attachment proof tests - the rotor head was installed in the
fuselage, and pulled with 12,000 pounds (simulating a 4G loading), passing
the test.
Thrust mount tests - the fiberglass structure through which all the propeller
thrust loads are transferred to the fuselage was proof tested at 6000
pounds (4 times the maximum expected thrust), and passed.
Propeller thrust tests - to determine the propeller RPM for takeoff,
we measured the thrust at full throttle at several different engine RPMs.
There was very little difference in thrust between 5250 and 5500 RPM -
about 1150 pounds of thrust at 240 horsepower. 5400 RPM was selected as
the maximum takeoff RPM. The propeller pitch at flat pitch was adjusted
so that the engine RPM cannot exceed 5400 RPM. Earlier tests to 6600 RPM
proved the propeller spar capable of 1.5 times the centrifugal load at
5400 RPM. (Static pull tests at 3 times maximum centrifugal force with
45 degrees of twist were also conducted.)
Rotor tests - the rotor was instrumented and tested at several RPMs,
looking at the cyclic control loads, the collective loads, the pylon movement
both fore/aft and side to side, the lift, flapping, and control system
hydraulic pressures. The maximum RPM reached with the propeller also running
was 540 RPM, at approximately 88 horsepower. Without the propeller, the
rotor went to 580 RPM (Mach .91) at approximately 145 horsepower. Compressibility
effects at the rotor tip were causing a steep increase in power required
for a small increase in RPM. Therefore, jump takeoffs will be performed
at 525 RPM (Mach .825).
Nosewheel Shimmy Tests - the nose gear was attached to a trailer towed
behind a truck. The trailer carried two 55-gallon barrels. The test was
performed at various weights and speeds up to 55 MPH, with the nose gear
at various stages of being raised and lowered. No shimmy was detected
in any condition. The nose gear tracked corners well.
Simulated jump takeoff tests - the rotor was prerotated to 525 RPM (3500
engine RPM) with the engine at full throttle, then the clutch disengaged.
The engine immediately goes to 5400 RPM as limited by the propeller. The
collective is pulled to hold at least 3500 pounds of lift. The cyclic
stick is moved in a circle until the lift decreases to 1000 pounds, at
which point the collective is returned to zero. The throttle is held full
open for one minute. Then the clutch is engaged for another cycle. 250
cycles like this were performed, with thorough inspections every 5 cycles.
On 1/20/98, on the 19th cycle, the guard support for the propeller drive
shaft pulley failed due to poor welding and went through the propeller,
destroying the version 3.4 propeller. The test stand was heavily damaged
but the rotor was not damaged. Testing recommenced on 2/20/98 with a new
prop and repaired test stand, and on 3/5/98, 250 cycles were completed.
All component proof tests have now been completed!
In Aircraft Engine Tests - the engine, drive train, and propeller were
tested in the aircraft in preparation for taxi tests. The engine cooling
on the ground was much better than expected. Even on a 90 degree day,
the engine could sustain 600 pounds of static thrust and short bursts
of 1200 pounds thrust without exceeding 210 degrees coolant temperature.
As intended, the propeller sucks enough air through the annular exit around
the spinner to effectively cool the radiator. Engine compartment temperature
actually dropped at full throttle, but immediately after shutdown, the
proximity of the exhaust to the fiberglass cowl caused smoking of the
cowl because there was no more cooling airflow. This required installation
of additional insulation. The propeller spinner began to fail due to hoop
loads pulling out the screws holding the spinner halves together. The
spinner is being fixed by bonding the two halves together and splitting
the spinner in the more conventional manner in the plane of rotation of
the propeller.
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