Archive of Weekly Updates
January - March, 2004
2004-03-29
- We ran the aircraft in the test pit to locate any problems, especially those associated with heat and the cooling system. After several cycles of running at full throttle until the water and oil temperatures reached 250 degrees (both occurred at about the same time), everything seemed to check out except that during one of the runs, the propeller drive belt failed. Examination of the belt revealed that the failure was due to excessive heat. We believe the source of the heat was the engine exhaust, which although insulated runs about 2 inches above and down one side of the belt. We installed an insulated heat shield between the belt and the exhaust to eliminate any radiating heat. Subsequent testing indicated this kept the belt from being any hotter than the engine block temperature.
- Installed the new prerotator yoke with a heat treat method that produced a tougher core. Proof tested the yoke to 3100 ft-lbs.
- Company president, Jay Carter, went to Washington, D.C. and made a presentation at the FAA Forecast Conference, a conference looking at the future of commercial and civil aviation. While in D.C., Jay also visited with several military and government personnel.
- Completed the molds for the internal shear webs and ribs of the scimitar propeller.
2004-03-22
- We took the aircraft to Olney for flight testing. On Wednesday, the pilots felt a vibration related to propeller rpm. The vibration was caused by an interference between the prop pitch mechanism and the thrust measurement system. The interference was caused by the thrust measuring system being low on oil, and the prop drive shaft being at a slight angle relative to the mounting bracket due to the belt change the week of 2/23/04. We modified the prop mounting bracket to put the shaft back in line with the bracket, and will more closely monitor oil levels in the thrust measurement system.
- We still had a problem of high oil temperatures (>220º F) in flight. We suspect that part of the problem is due to the installation of one of the oil coolers, where the airflow into the cooler is not uniform. We are modifying the oil cooler installation to ensure a more uniform airflow to the cooler.
- Modified wiring to improve radio communications.
- Added two new pages of information to main pilot display.
- Created a new warning for the landing gear, which warns the pilots if the gear is taking too long to extend because of the drag on the gear due to airspeed.
- Laid up the leading and trailing edge spars of the scimitar propeller. Began work on the plugs for the internal shear webs.
2004-03-15
- We have added a new page to the website, Frequently Asked Questions about the CarterCopter. The page answers many of the common questions people have about the CarterCopter, and will hopefully clear up some misconceptions about the aircraft.
- When we tested the aircraft in the test pit with the new prerotator yoke, the part failed, this time at a lower load than the previous design. Examination of the broken part revealed that the new method of heat treating made the part very fragile. We have machined a new yoke using a different steel alloy, which will be heat treated with a method that will leave the core tougher. Since the prerotator is used only on the ground, and is not under load in flight, we installed a spare of the current fragile yoke to use until the new, tougher yoke is completed. We will limit prerotator drive torque to keep the part from failing.
- Modified automated control programs to improve operation.
- Completed the root block of the main spar for the scimitar propeller. Made the tooling to align the main spar in the skins. Completed the leading and trailing edge spar molds.
2004-03-08
- After examining the rotor head, the prerotator yoke was the only part that needed to be replaced because of last week's prerotator failure. We talked with a metallurgist about the part, and it turns out that the method of heat treating that we had used on the part was very prone to cracking. We think that the part had cracks introduced during heat treating, which caused high stress concentrations, with the torque spike during rotor stopping being a contributing factor. We redesigned the yoke with a larger fillet to reduce stress concentrations, had it machined, heat treated with a different process, and installed back into the aircraft, all in one week. We have also modified our rotor stopping procedure to eliminate the large torque spike when the rotor stops.
- Modified the cyclic links to give more spindle travel.
- Modified the collective links and linkages to give more collective travel.
- Made a simpler manual override for the automated collective control, allowing the pilots to easily pull more collective on landing if they want to.
- Laid up the upper and lower skin for one blade of the DARPA funded scimitar propeller; completed the leading edge and trailing edge spar plugs; and laid up the root block of the main spar.
2004-03-01
- We took the aircraft down to Olney for flight testing. We had several
good flights on Thursday. The pilots performed several simulated landings
at altitude, and the automated controls worked wonderfully. Our best
rate of climb with the landing gear extended was 750 fpm.
- On the last flight on Thursday, the engine quit running in flight,
just as suddenly as if the pilots had turned off the ignition. The aircraft
was at 1200' AGL, so the pilots had their choice of runways. They made
a nice dead stick landing without cyclic or collective hydraulic boost.
Thanks to the backup air boost, the controls were still very manageable.
Inspection on the ground after the incident revealed that wires connecting
the engine crank sensor to the engine computer had become too hot, melting
the insulation and shorting the wires. Without the signal, the computer
could not control the engine. The wires were repaired and wrapped with
thermal insulation.
- During spin up prior to taxiing for our first flight on Friday, the
prerotator u-joint yoke failed. We believe that the yoke cracked the
previous day, when we enaged the prerotator with the engine off to stop
the rotor from spinning. Right at the instant when the rotor stops,
a very large torque is generated- much larger than our operational torque
when prerotating the rotor. We have redesigned the yoke with a larger
fillet to reduce the stress concentration, and have modified our rotor
stopping procedure to eliminate the large torque spike. Once we disassemble
the rotor head this week, we will know the extent of the damage. The
prerotator is only used on the ground to spin up the rotor, so it would
not have failed in flight, nor is it a necessary system in flight. We
are also running the prerotator system at a higher stress level than
originally designed, since we are using a larger rotor than the original
CarterCopter rotor.
- Completed the final bonding operation on the second blade of the DARPA
funded extreme mu rotor.
- Laid up the spar for the DARPA funded scimitar propeller. This was
the first spar we have designed using the three dimensional solid drafting
program, Solidworks, which we used to design the spar and its mold,
and to calculate the number of carbon strands needed to lay up the spar.
The mold was machined on a five axis CNC machine using an electronic
file generated by Solidworks. This was the smoothest layup operation
we have ever had for a spar.
- Began preparing the molds and making templates to lay up the blade
skins for the DARPA funded scimitar propeller.
2004-02-23
- Finished tuning the engine with the turbo. Peak power was 385 HP
at 4800 rpm and 2.5" of boost pressure.
- After tuning the engine, an inspection of the propeller drive belt
revealed that it was beginning to split, even though we had kept horsepower
down from the previous week's tests when we failed the belt. We decided
to go back to a belt system which we had used in the past which has
a higher capacity. This meant changing the drive pulleys, as well as
modifying several brackets to accomodate the new center distances necessary
between the pulleys.
- Began replacing the numerous Molex connectors in the aircraft's wiring
system with more reliable AMP connectors. Because of the large number
of connectors, this will be an ongoing process.
- Completed all of the internal components of the second blade of the
DARPA funded extreme mu rotor, and bonded them to the lower skin of
the blade. We expect to bond the upper skin to the blade this week.
2004-02-17
- Made a modification to the newly installed oil thermostat.
- Reassembled the rotor head after making the several modifications
already noted in last week's update.
- Made several modifications to the automated control software to improve
its operation based on lessons learned in flight testing.
- Began tuning the engine with the turbo. Partway through the tuning
process, the prop drive belt failed. We are going to examine the aircraft
this week to determine the cause of the failure. We currently suspect
two possibilities- either that the pulleys were misaligned or that we
put too much power to the belt at too low of an rpm. If the failure
was due to overloading the belt, we will limit the turbo boost pressure
to keep horsepower lower, and will consider installing a different set
of pulleys and belt to give us a greater capacity.
- Took the first blade of the DARPA funded extreme mu rotor out of the
blade molds. Laid up the skins for the second blade.
2004-02-09
- Reinstalled the turbo. We expect to put the aircraft in the pit this
week to calibrate the engine and check the other modifications we have
made. We hope to be back in Olney for flight testing by the end of the
week.
- Installed a redesigned oil thermostat. This will keep the oil going
to our boosted controls at a constant temperature independent of the
outside air temperature.
- Modified the rotor head to allow more clearance between the collective
control tube and the prerotator u-joint. There had been a problem of
interference between the two when the pylon was forward and the pilot
pushed forward on the stick.
- Installed strain gauges in the rotor head to measure rotor lift and
collective control force.
- Completed the final bonding operation of the first blade of the DARPA
funded extreme mu rotor.
2004-02-02
- We spent three days flight testing in Olney, without the turbo installed
on the engine. Our goal was to gather data on the automated controls,
which appear to be working wonderfully. The automated collective pitch
control worked great for takeoff and cruise through 142 mph. It appears
that it will work for automated landings as well, but since we were
not able to practice any simulated landings at altitude due to a low
ceiling, we continued to do conventional landings by manually operating
the collective. The automatic rotor rpm control also appeared to function
correctly, tilting the spindle back 50% of its travel at 140 mph to
maintain the rotor rpm at 150. We did not stay at this speed long enough
to confirm that the controller would continue to be stable. Our best
rate of climb during these tests due to the reduced horsepower available
from the non turbo charged engine (12 lb. aircraft weight per hp) was
500 ft/min at 100 and 110 mph with the gear extended, and the fastest
we went was 142 mph (mu of 0.63). Once we adjusted the blade pitch to
get the rotor to track, our pilots reported that the aircraft was ultra
smooth. With their eyes closed, there would have been no clue that they
were in a rotary wing aircraft. We plan to continue flight testing in
one to two weeks once we reinstall the turbo. Our climb rate will be
significantly better, and we should be able to start expanding the speed
envelope.
- We installed an additional oil cooler, which should keep our oil
temperatures fine even on hot days, but our oil thermostat did not function
correctly. The temperature it sensed was more influenced by the cool
oil coming from the oil coolers than from the hot, bypassed engine oil,
so the thermostat sensed a temperature cooler than the engine oil and
continued bypassing the oil coolers most of the time, keeping the engine
oil temperature high. We were forced to remove the thermostat in order
to complete the flight test. We will install a redesigned thermostat
before flying again.
- We experienced a problem trying to extend the landing gear at 110
mph. The drag on the landing gear was high enough to open a pressure
relief valve in the gear's oil lines. Once the craft slowed to 80 mph,
the drag was low enough that the gear extended. We will increase the
preset pressure on the relief valve before future flights.
- Finished all the tooling and internal parts for one blade and began
the final bonding operation of the first blade of the DARPA funded extreme
mu rotor.
2004-01-26
- Removed the failed turbo and sent it off for a failure analysis.
Failure was due to a lack of oil to the bearings caused by blockage
of a flow control needle valve due to Teflon tape. Received a rebuilt
turbo.
- Recalibrated the engine controller for natural aspiration. The engine
without boost produces only 340 HP at 5200 rpm. (At 1 psi boost the
engine produces over 400 hp).
- We may fly some this week if our rate of climb with the reduced hp
is at least 500 ft/min. Test weight without the turbo installed will
be about 3900 lbs. Our intention is to continue to check out and tweak
the automatic controls – initial take-off collective pull, initial
rotor rpm energy management, cruise rotor rpm, and rotor flapping (maintain
balanced lift moments between the advancing and retreating blades).
Next week while our copilot is on a skiing vacation, we plan to reinstall
the turbo with a few modifications.
- Modified the collective boost system to remove the dead band regardless
of the load direction.
- Modified the flapping sensor so that it measures only flapping due
to lift differences between the advancing and retreating blades, and
not due to spindle movement.
- Completed the trailing edge spar for one blade of the DARPA funded
rotor.
- Finished casting second blade tip weight, cut and machined the tip
weights for both blades and laid up the carbon uni pockets for the first
blade weights.
- Held our annual shareholder's meeting over the weekend.
2004-01-19
- President Jay Carter spent another 2 days in Washington, D.C., meeting
with government and industry.
- Replaced prop drive pulleys. Used a harder surface coat to keep them
from wearing as rapidly.
- Increased the inner diameter of the hoses and fittings connecting
the oil cooler to reduce its pressure drop and increase the engine oil
pressure.
- Designed, built, & installed an oil cooler thermostat.
- Recalibrated the engine computer for 400 HP at 1 psi boost.
- The harmonic balancer & drive pulley came loose at max horsepower,
causing the belt to ride up over the pulley, failing part of the belt.
The engine was shut down from max horsepower to a stop and zero oil
pressure in less than 4 seconds. The turbo continued to spin down without
oil pressure and failed its bearings.
- We plan to fly the aircraft without the turbo until the turbo can
be replaced. This engine should be capable of producing nearly 400 HP
with natural aspiration.
- Hired a second electronic/mechanical technician- Alex Dobek.
- Completed mold for the trailing edge spar of the DARPA funded rotor.
- Laid up shear webs for the DARPA funded rotor.
2004-01-12
- We have found the cause of our sudden loss of oil pressure- the rear
main bearing had spun. This was due to too low of an oil pressure (50
psi) and too high of an oil temperature (235 degrees) for the given
load on the bearing. The bearing sees a higher load than in an automobile
because of the overhung drive pulley load. The crankshaft also had a
crack at the corner of the main bearing and the throw. The Auto Shop
had finished rebuilding the larger, 427 cu. in., racing version with
a stronger, forged crank, so we can now install that into the aircraft
while we decide what to do with the smaller, basically stock 347 cu.
in. engine. To keep oil temperatures lower, we are going to install
an additional oil cooler.
- The drive belt wore through the hard anodize on the drive pulleys,
and had begun to eat into the pulley teeth. We have machined new pulleys,
and are using a different surface treatment to improve their wear resistance.
- Finished the molds for the internal shear webs of the DARPA funded
rotor.
- Made the plug for the trailing edge spar of the DARPA funded rotor.
2004-01-05
- We have not yet determined the cause of the oil pressure drop described
last week. After a partial dissassembly of the engine, not including
removal of the turbo exhaust system, the prop drive nor a number of
other components, we thought we had found the cause. An 1/8 in. gap
in the oil suction tube had been sealed with silicon, instead of an
o-ring as designed, which could have caused a leak. Repairing this did
not correct the problem. This week, we are going to completely dissassemble
the engine, including those components that were not included last week,
to determine the cause of the pressure drop.
- Repaired nose gear. During transportation on the trailer, one of
the supports broke loose from the fiber glass because of the way the
aircraft was tied down. This is not the type of load the landing gear
would experience in flight operations.
- Added an air/oil separator tank below the turbo to ensure that the
oil does not back up in the turbo and get lost in the exhaust or compressor.
- Installed an oil pump pressure relief to the auxiliary oil pump to
keep the pressure from getting too high on cold weather starts.
- Moved turbo air inlet to the top of the engine compartment, which
should decrease inlet temps by about 15ºF.
- Stiffened the oil pump support.
- Made the plugs for the internal shear webs of the DARPA funded extreme
mu rotor.
- Carter receives its first Publication Cover! The first published photo
of the newly restored CarterCopter will appear on the cover of the 1st
January issue of Trade-A-Plane (TAP). The TAP Cover photo was taken
during recent flight-testing in December. Trade-A-Plane has more than
132,000 readers and has been the leading aviation marketplace publication
for more than 60 years.
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